Car-and-Safety.com
Ford Mustang Power Train Safety Report | Aug 27, 2011
Reported on Aug 27, 2011
(NOTE: CAR IS A MUSTANG GT 5 LITER) THIS INCIDENT FOLLOWED MY INITIAL DRIVETRAIN COMPLAINTS TO MY LOCAL DEALERSHIP AND THEIR REPLACEMENT OF MY CLUTCH PEDAL ASSEMBLY. ENTERING A HIGHWAY, I APPROACHED A SPEED OF APPROXIMATELY 75 MPH IN 3RD GEAR, TAKING THE ENGINE CLOSE TO 6K RPM. WHEN ATTEMPTING TO SHIFT INTO 4TH WITH THE CLUTCH PEDAL FULLY PRESSED TO THE FLOOR, THE STICK WOULD NOT BUDGE INTO THE 4TH GEAR SLOT. AS THE CAR WAS SLOWING DOWN, I TRIED OTHER GEAR SLOTS: 5TH, THEN 6TH, 4TH AGAIN, TO 3RD. NOTHING. FINALLY, I REMOVED MY LEFT FOOT FROM THE PEDAL ALTOGETHER AND NOTICED THE PEDAL WAS STUCK TO THE FLOOR. AFTER PUMPING IT TO NO AVAIL, I WEDGED MY FOOT UNDER THE PEDAL TO KICK IT BACK UP. MY DRIVETRAIN WAS ONCE AGAIN RESPONSIVE. I WAS ALREADY AWARE OF A RUMOR THAT LATER MODEL MUSTANGS HAD HIGH RPM GEAR-SHIFTING ISSUES, BUT THIS WAS THE FIRST PERSONAL OCCURRENCE FOR ME. BASED ON THIS SUSPICION, I ATTEMPTED TO RECREATE IT ON THE WAY BACK HOME AND I WAS ONCE AGAIN ABLE TO FREEZE MY CLUTCH TO THE FLOOR. MY CAR IS CURRENTLY IN FOR REPAIR, AND I BELIEVE THEY ARE REPLACING THE CLUTCH AND PRESSURE PLATE FOR THEIR NEXT FIX ATTEMPT. *TT | |
Make: | Ford |
Model: | Mustang |
Manufactured by: | FORD MOTOR COMPANY |
Year: | 2011 |
Was a crash reported? | N |
Was an injury reported? | |
Was a death reported? | |
Was a fire reported? | N |
Location: | OKEMOS MI |
Vehicle Identification Number (VIN): | 1ZVBP8CF4B5 |
Mileage: | 10800 miles. |
Speed: | 75 MPH |
Number of cylinders: | 8 |
Vehicle type: | RWD |
Vehicle fuel: | GAS |
Was a police report filed? | N |
Tire size: | |
Dealer name and location: | |
Previous Report:Power Train | Next Report:Electrical System |